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GTi not starting problems, does crank

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  • GTi not starting problems, does crank

    Hi all, 99 GTi 1.8T AGU
    Yesterday I installed a Diverter Valve because when bought the car it didn’t have one (crazy I know). It has a fmic and cold air induction with silicone intake.
    I recently have replaced the valve cover gasket as I was getting oil on the spark plug wells but didn’t start it till I had the DV installed.
    Sooooo, took it for a short test run and only got to second gear when the engine lost power and died on me. When I changed from 1st to second it made a backfire type sound but I don’t think it was a backfire (not as loud).
    I towed it back into my garage but still can’t get it started (does turn over). I have also recently replaced the following: crank angle sensor, coolant temp sensor, ignition amplifier, spark plugs.

    Any help is appreciated

  • #2
    Ground or wiring issue from removing the valve cover?

    Does it have fuel? Does it have spark?


    Sent from my iPhone using Tapatalk

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    • #3
      I’ll clean up the ground and see if that helps... yes has spark but will check the fuel pump relay also

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      • #4
        From what you have said. It kinda sounds like the fuel to air might be too lean. Have you made any mods to the ECU settings ?
        Matthew.
        https://www.DomainRegistrationDns.com.au
        DomainRegDnsAust@gmail.com

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        • #5
          No ECU mods that I’m aware of, I’ve only had the car for a few months. I find it really strange that adding in the diverter valve is the only real change and the gear shift made it die

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          • #6
            Is the diverter stuck open?
            optimumcode@gmail.com | https://www.vwwatercooled.com.au/for...i-;-79012.html | https://www.facebook.com/TTY-Euro-107982291992533

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            • #7
              Ok, so it was running rich so checked all of the intercooler pipes and found one had come loose. Thanks for all of the replies, it’s now running great.

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